Liang Hongjun, Deng Xingde, Jia Lichang, Xu Zhixiong. DOWN HOLE TROUBLE SHOOTING TECHNIQUES IN KC-1 WELL[J]. Oil Drilling & Production Technology, 1997, 19(3): 35-39. DOI: 10.3969/j.issn.1000-7393.1997.03.008
Citation: Liang Hongjun, Deng Xingde, Jia Lichang, Xu Zhixiong. DOWN HOLE TROUBLE SHOOTING TECHNIQUES IN KC-1 WELL[J]. Oil Drilling & Production Technology, 1997, 19(3): 35-39. DOI: 10.3969/j.issn.1000-7393.1997.03.008

DOWN HOLE TROUBLE SHOOTING TECHNIQUES IN KC-1 WELL

  • KC-1 well is located in Klasu reservoir, Kuche Depression, Tarim Basin.This is a most completed and deepest well with a complex of different pressure systems in the Basin. In its drilling process, 10 overflows, 51 lost circulation’s and other down hole accidents were encountered. As the trouble shooting measures, a series treatments such as back pressure method and engineer method well killing, regular and cement-gel lost circulation plugging operations were applied. At last, the well was drilled out successfully to its designed final depth.
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