龚志敏. 乡1井钻盐岩层技术分析[J]. 石油钻采工艺, 1995, 17(4): 40-43,87. DOI: 10.3969/j.issn.1000-7393.1995.04.006
引用本文: 龚志敏. 乡1井钻盐岩层技术分析[J]. 石油钻采工艺, 1995, 17(4): 40-43,87. DOI: 10.3969/j.issn.1000-7393.1995.04.006
Gong Zhimin. TECHNICAL ANALYSIS OF XIANG 1 WELL DRILLED THROUGH THE HALITE FORMATION[J]. Oil Drilling & Production Technology, 1995, 17(4): 40-43,87. DOI: 10.3969/j.issn.1000-7393.1995.04.006
Citation: Gong Zhimin. TECHNICAL ANALYSIS OF XIANG 1 WELL DRILLED THROUGH THE HALITE FORMATION[J]. Oil Drilling & Production Technology, 1995, 17(4): 40-43,87. DOI: 10.3969/j.issn.1000-7393.1995.04.006

乡1井钻盐岩层技术分析

TECHNICAL ANALYSIS OF XIANG 1 WELL DRILLED THROUGH THE HALITE FORMATION

  • 摘要: 1井是塔里木盆地的一口深探井,在5166~5331.38m二迭-石炭系地层钻遇复合盐岩层,多次发生漏失和阻卡,井下情况极为复杂。通过对该共复合盐岩层蠕变规律的分析,优化了钻井液类型和性能。认为地层破裂压力值偏低(1.61~1.65g/cm3).钻井液密度不能太高,因此只能用不太高的钻井液密度和欠饱和盐水(氯根含量为180000~185000ppm)钻井液体系来控制盐岩层的蠕变速度。结果,钻进比较顺利。本文介绍了乡1井钻复合盐岩层的经验和教训。

     

    Abstract: XING 1 well in Tarim Basin is a deep exploration well. While drilling through the Permo-Caboniferous formation,a composite salt formation was encounted from 5 166m to 5 331.38m,and then lost circulation and drill pipe sticking occured many times and the down hole condition was very complex. Drilling fluid types and properties were optimized,by analyalng the creep properties of the composite salt formation. Formation breakdown pressure was thought to be rather low (1.61~1.65g/cm3 ),so only low density drilling fluid and undersaturated salt-water drilling fluid system (chlorion content of 180 000~185 000ppm) could be used to control the creep rate of the salt formation. The result proved to be successful. This paper recommened the experience and lessons got from drilling XING 1 well through the composite salt formation.

     

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